Atom Motion motors work inconsistently
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I'm noticing that even with the example sketch (https://github.com/m5stack/M5Atom/tree/master/examples/ATOM_BASE/ATOM_Motion) the two motors (pins M1, M2) turn inconsistently. Sometimes a positive speed (+100) will result in motion, and likewise with a negative speed (-100). But just as often the write will result in a high-pitched tone from the motor, but no motion. Writing zero always stops both motors. Has anyone else experienced this, and can you offer any insight/ideas?
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@toastedcode did you figured out programming m5stack tough unit. I am newbie and looking for some help on programming it by block diagram in webui
Specifically looking to connect rs485 sensor output from my water level device and pressure transducer thenconvey data by matt to server
Any help or step by step programming video would be great
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